G4APV's EB104
Construction Page
EB104
This
web page
contains a whole load of stuff about the construction of a MRF150 based
600W linear amp. The basis of the amp is an old but reliable
design by Motorola that came out as Engineering
Bulletin 104,
hence EB104.
If you want the ShackCam then click here.
Case
The
case came from Maplin.

Parts
So what goes into the case? Here is the kit of EB104 parts
that I
got
from Communication
Concepts for the amplifier
itself:

Attenuator
As
well as that I needed a few other parts, these are for the
attenuator to drop 20W down to 6W. This 6dB odd loss ensures
that
most HF transceivers with a typical low power output of about 10W can
be used to drive the amplifier with a bit of a margin of safety.
It also ensures the input impedance to the amplifier is more closely
controlled. The parts came from mainly from JAB
components.

Hardware
I
quickly came to the conclusion I would need quite a few nuts, bolts and
other hardware. I used M3 and M4 nuts and bolts as they
fitted the devices.. This lot came from Farnell:

Thermal Issues
WIth 600W out and about 60% efficiency then there is as much as 400W to
get rid of. This means getting the heat away from the devices
with a copper spreader and then getting rid of it with a heatsink.
Both the
spreader and the heatsink also came from Communication Concepts:


I was not confident about pure convection and so went for forced air
cooling using mains fans, again from Ebay.
Power
Supply
The
amplifier
runs of 50V and with 600W out will need about 1000W in, ie 50V at 20A.
To
power
this an ELTEK
brand new power supply off Ebay
but sold by Anchor
Surplus
in Nottingham is ideal. It is nicely protected and can be
started
up by a 5V control line. This allows it to be powered down on
receive to avoid nasty noises from the switching, although n practice
it seems to reasonably quiet anyway:

Auxiliary Power
I decided to use 12V for control systems to provide compatibility with
other systems I had. I got a 12V PSU, again off Ebay, shown
here
with
the cooling fans.:

If
you
are really interested (or is it sad?) then here is the
spreadsheet with all parts as
ordered
(except Ebay).
Main
Board Assembly
Before the board can be assembled, there is a great deal of mechanical
work to be done to mount the heat spreader onto the heatsink and then
mount the unpopulated PCB onto the spreader. Only when all of this is
done is it appropriate to put the components onto the amplifier board.
After much planning, drilling and tapping here is the PCB on the
spreader, with the spreader, on the heatsink. I found it
critical
to have a pillar drill to do this. I went and bought a
£55
one, new, from Machine Mart.
Here's the trial of the board on the spreader and heatsink:

Population of Board
This
a fairly long winded process with components on the top and the bottom
of the board. On the bottom of the board are some chip caps.
The board needs to be just clear of the spreader to ensure
these
don't short:

I next fitted the solder pins, and in retrospect the two big resistors
that are part of the feedback loop (below) should have been on pins, it
would make life much easier later on:

Putting the rest of components on gives:


Power
Devices
After various trial fittings, marking out, drilling and tapping of the
spreader and finally checking for shorts, the board was fitted to the
heat spreader and the devices soldered in:

Notice the 1W resistors have got a bit bent to allow access to the
device screws. Next time they will go on solder posts.
Initial
Testing and Bias Setting
At this point I decided to be brave and put the supply on and,
hopefully, set the bias currents. I bodged up a 3A fuse (just
because I had one) and monitored both the voltage and the current.
I am fortunate to have a 0 - 50V, 40A variable PSU
which
makes life easier. Here is the bodge up of the first test:

It proved to be pretty easy to set the bias current to 1A total, ie
250mA per device. As I was taking it up from the initial
supply
voltage of 40V to 50V as a check there was a bang, a blue flash and a
blown fuse - not good. It turned out to be a small offcut
strand
of wire across one of the devices. There is a lesson here
about
cleaning the board before testing!
Gain
Test
The next check was to see if it amplified. I used a signal
generator which has a maximum output of 19dBm (ie about 100mW) at 14MHz
to see what would happen. Thsi produced about 5 or 6W into a
50
Ohm dummy load which seemed ok to me. The next check was to
use
an FT817 (out of picture) to provide some RF as this can have it's
output reduced down to about 100mW.

Attenuator
Board
Once I had established the amplifier board itself seemed to be working,
I designed the attenuator. The actual design of the component
values was done using WinAtt
from GM4PMK on G3SEK's webpages. I used TinyCAD
for the schematic capture, FreePCB
for routing the board and ViewMate
to
print to pcb out.
I
got
the board made at
work using a prototyping system that uses a routing technique to
remove copper from those areas where it is not wanted:

Another idea I investigated but did
not
really got to work properly is the
"iron
on" technique. The finished, routed boards come out ok, but
are obviously not plated, but that I can live with:

Here
it is populated, fitted but not
yet wired in:

I
then bodged on an output
transmit/receive relay and the 12V power supply to give a complete
working system:

Output
Switching
and SWR Board
To
protect the devices it is clearly
necessary to shutdown the amplifiier in the event of high SWR, for
example a flashover in an ATU. Also a relay for
transmit/receive
swithching ant the output is needed. I then designed a board
to
do this, it removes the 50V bias supply if it detects excessive SWR at
the output:. The PCB
layout starts as a schematic capture and is then imported into EasyPCB
to give "ratlines":

The
final result looks like:

Mounting
in the
Case
Much
of the time was spent puzzling
out how to mount all the bits in the 19" rack mount case.
Here is
the stage with the amplifier, input and output boards and power
supplies mounted. The cooling fan, output filters and front
and
rear panels have not yet been dealt with.

Here are the major components
installed and wired up. The amplifier is now usable but is minus
the output filters. Some low level instability in the amplifier
disappeared with the input and output SO239 and fitted and the power
supplies properly wired in

At this stage the lack of filters means the output was not
too clean, this was on 80m, some harmonics are only some 25dB down on
the fundamental:

The other lesson is not to push things to hard. The bypass caps
on the drains supply don't like too much RF current. While trying
to see how much power I could get out of it I discovered they go bang
and burst into flames. Here is the aftermath of this happening,
the remaining leads in the plated through board were very difficult to
remove.

It seems as if too many harmonics are the problem which leads nicely
into the design of the output filters.
Filters
It seems to be fairly well established that a 5th order Chebyshev
design is appropriate for removal of harmonics from power amplifiers.
The design of the filters was based on the ARRL Standard Value Capacitor
(SVC) tables. Once the values had been calculated they were
modelled using ELSIE. Using information I already had (not
sure where it came from) it became clear that a T-130-2 ferrite would
handle the power and provide the necessary inductance. An example
of the design process is given in this document.

I put together a prototype of the
3.5MHz filter as well as simulating
it: I then used a Panasonic VP-8191A signal generator plus a
HP8590A
spectrum analyser set to peak hold to find the filter's response:

I decided to put 3 filters on a PCB
and then use 2 boards to cover all bands. This was in an attempt
to keep the track lengths acceptable. It seemed a bad idea to
have lots of RF going down long tracks. The higher the frequency,
the shorter the track ought to be. I used an earth plane approach in attempt
to cope with the potentially high RF currents. The unpopulated boards look like:

And once populated and the topband filter tested:

The second board was built and tested. I then stacked them using
some M3 studding and wired it all up:

These photos also show the tray made out of bend and painted steel that
carries the boards and acts as a duct for the cooling air. The
left hand side where the space is is where the control board will
eventually go.
Using the amplifier on 160m
and 80m at about 350 - 400W it
developed a fault where it would become erratic on transmit. The
power output would disappear and then reappear. This did not
appear to be related to band, drive level, output power level etc.
At this stage I bodged on some meters to watch the supply voltage
and current (see below). Of course it did not do it again
although I did
get it to smoke while giving it a long wwwaaaahhhhh. I suspected
that the PSU was going into some sort of shutdown, but not due to over
current as the drive level did not affect the problem. I
suspected
RF getting into the control circuitry of the PSU.

Monitoring the voltage and
current
soon showed the problem was not the PSU. Putting an old SWR
bridge
onto the input showed a very poor match and that the drive from the
IC735 was disappearing when the problem occurred. My conclusion
is
that rig was shutting down as it got warm due to a poor mismatch (or is
that a double negative?). The solution is to run the IC735 via
the 6dB
input attenuator so that it always sees a good match. The problem
has
not happened again since keeping the attenuator in all the time.
However the filters do seem to be working, the second harmonic is now
some 45dB down on the fundamental on 80m. Compare this to the
earlier plot of no filter which had the fundamental only 25dB down.
The filter should, at about 7.5MHz provide about 20dB of
attenuation so, surprisingly, it seems to do wha the theory says it
should! The third harmonic now seems to have gone - good.
This is still work in progress as I
continue to build the amplifier.
Bob
Harris, G4APV, 31st August 2009